Even then though it still has a miss, Im not sure if this has anything to do with the vacuum hoses all being blocked off or something else.
I changed the plugs and no change, I played with the timing and no change either. I haven't tried changing the leads yet but Ill give that a try next time I go there. Also I didn't think of looking at the dizzy cap or rotor until now.
I understand a vacuum leak will cause a misfire also but I have no way to check or sort out all the vacuum hoses. There is about 20 cut off ends with screws/bolts in them and I even noticed a outlets/inlets from the carby without any hoses on it at all.
Ill check what I can in the next few days but any advice would be appreciated, I can get more pictures if needed.

